Sunday, July 24, 2011

Oil & Gas Spill Of the Day +/- 210,000 Gallons of Produced Water - Arapahoe County Colorado

RENEGADE OIL & GAS COMPANY LLC 
This post is a very comprehensive look into the history of one company's well site and its track record.  It appears that a large discharge of produced water occurred in late 2005. Was this spill a concern? It is 'estimated' that +/- 5,000 barrels of produced water discharged on the ground surface and into Cottonwood Creek. According to COGCC documents, one barrel equals 42 US gallons.  Five thousand barrels equates to 210,000 gallons of produced water that was reportedly spilled into Cottonwood Creek.  Was this company fined? Why has this company had so many unsatisfactory inspections/violations and is still being allowed to manage an active well?  Should they be fined? Should they be shut down for having so many violations? 

Do all companies get 'breaks' for their violations? Are O&G violation rules different if a well is located on BLM land? Where did the produced water go? Does the Community Right-To-Know Act of 1986 apply?

Click 'Read More' at the bottom of this post to view images and documents.
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Date Rec'd: 12/21/2005 Report taken by: BOB CHESSON
DocNum: 1433324 API number: 05-005 -06522 Facility ID: 204437

Operator Information

Operator: RENEGADE OIL & GAS COMPANY LLC Oper. No. 74165
Address: P O BOX 460413 ATTN: EDWARD INGVE AURORA , CO 80046-0413
Phone: (303 )680-4725 Fax: (303 )680-4907
Operator Contact: JB CONDILL

Description of Spill:

Date of Incident: 12/1/2005
Type of Facility: WELL
Well Name/No. STATE 2 Fac. Name/No.
County Name: ARAPAHOE
qtrqtr: NESW section: 36 township: 4S range: 58W meridian: 6

Volumes spilled and recovered (bbls)
Oil spilled: 0 Recvrd: 0
Water spilled: Recvrd: 0
Other spilled: Recved:

GW Impact? N     Surface water impact? Y     Contained within berm? N


Area and vertical extent of spill: 20-FT X 800 -FT
Current land use: RANGELAND
Weather conditions:
Soil/Geology description
Distance in feet to nearest surface water:
Depth to shallowest GW:
Wetlands: Buildings:
Livestock: Water Wells: 

Cause of spill:
EQUIPMENT FAILURE

Immediate Response:
BACKHOE PLUGGED HOLE IN BERM AND REINFORCED BERM
Emergency Pits:
NONE
How extent determined:
VISUAL
Further Remediation
REMEDIATION UNDERWAY.
Prevent Problem:
REVIEW OF ALL COMPANY POLICIES WITH EMPLOYEES.
Detailed Description:
INSPECTION BY COGCC STAFF IN RESPONSE TO SURFACE OWNERS CONCERN IDENTIFIED A BREACH IN THE PRODUCED WATER PIT ALLOWING PIT TO DISCHARGE TO DRAINAGE OF COTTONWOOD CREEK AT A RATE OF APPROX. 3 GPM. RELEASE ONGOING FOR SOME TIME SO ESTIMATES OF RELEASE ARE VERY APPROXIMATE (5,000 BBLS (?).)

 
Field Visit/Follow Up
Name Phone Date
No Field Visit data found.

 
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SPILL IS REMEDIATION NO 3588.




Historical field inspections at this specific well



API Number: 05-005-06522
Name: STATE #2
Location: NESW 36 4S 58W
Lat: 39.65898 Long: -103.82827
Operator #: 39100

Field Inspections:

Inspection Date: 5/24/1995

Inspection was: No Satisfactory/Unsatisfactory Indicator

Violation: Y

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
HISTORICAL
WELLSIGN POSTED BUT ILLEGIBLE, PRODUCING AT TIME OF INSPECTION PUMPING UNIT FENCED, LOCATION IN REASONABLE CONDITION OIL SATURATED SOIL AROUND WELLHEAD




Inspection Date: 5/25/1995

Inspection was: No Satisfactory/Unsatisfactory Indicator

Violation:

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
HISTORICAL
PRODUCED WATER PIT BERM HAD BEEN REPAIRED, BUT EVIDENCE OF DISCHARGE OF WATER & OIL STILL EVIDENT FROM TANK BATTERY EAST IN DITCH ALONG ROAD TO CONFLUENCE W/ COTTONWOOD CREEK, THEN NORTH IN COTTONWOODCREEK, OTHER PROBLEMS INCLUDE BERMS AROUND TANKS TOO SMALL, ABANDONED PIT, DRUMS. WILL WRITE LETTER TO AL POWELL RE REQUIRED REMEDIATION



Inspection Date: 12/1/2000

Inspection was: Unsatisfactory

Violation: Y
Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
ACTION
REMOVE OIL FROM PIT AND REPAIR SCREEN TO PREVENT WILDLIFE ACCESS. CLEAN UP OIL SATURATED WEEDS.
FIREWALL
TANK BERM APPEARS ADEQUATE
GENHOUSE
OIL SATURATED WEEDS AROUND PIT
TANKBAT
(3) 300 BBL PROD TANKS
WELLSIGN
SIGN POSTED AT WELL AND BATTERY


 
 
Inspection Date: 7/11/2001

Inspection was: Unsatisfactory

Violation:

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
ACTION
2ND NOTICE- REMOVE OIL FROM PIT AND REPAIR SCREEN TO PREVENT WILDLIFE ACCESS. CLEAN UP OIL SATURATED WEEDS.
GENHOUSE
OILY WEEDS AND SOIL AROUND PIT
MISC
PUMPJACK OPERATING DURING INSPECTION
WELLSIGN
SIGN POSTED AT WELL


 
Inspection Date: 7/25/2001

Inspection was: Satisfactory

Violation: N

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
FIREWALL
TANK BERM APPEARS ADEQUATE.
TANKBAT
OPERATOR SET STEEL TANK TO REPLACE SKIM PIT.


Inspection Date: 12/1/2005 ***(see reports and images below pertaining to the recorded discharge)

Inspection was: Unsatisfactory

Violation: Y

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
ACTION
CORRECT PIT BREACH ASAP. DISCHARGE IMPACTED AREA WILL REQUIRE REMEDIATION.
GENHOUSE
DISCHARGE FROM PIT MUST BE TERMINATED IMMEDIATELY. OTHERWISE TB LOCATION GENERAL HOUSEKEEPING OK.
SPILCOM
BREACHED SOUTH PIT WALL (SIGNIFICANT EROSION) ALLOWING DISCHARGE OF PRODUCED WATER TO DRAINGE TO SOUTH. SIGNIFICANT VEGETATION GROWTH IN SPILL AREA INDICATES LONG-TERM RELEASE NOT RECENT DISCHARGE.




Inspection Date: 9/18/2007

Inspection was: Unsatisfactory

Violation: Y

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
ACTION
NOAV ISSUED. REMOVE OIL FROM PITS. REPAIR ALL LEAKS. REMOVE OIL-SATURATED SOIL FROM WELLSITE, BATTERY AND PITS. REMOVE CONTAMINATED BERMS. RE-BUILD PIT BERMS. COVER SKIM PIT. REMOVE MISC. JUNK.
FIREWALL
BERMS OK AROUND BATTERY TANKS. BERMS AROUND PITS MIXED WITH OIL PULLED FROM PITS - CONTAMINATED.
GENHOUSE
MISC. JUNK ON WELLSITE. LEASE ROAD TO BATTERY IN DISREPAIR.
MISC
PUMP JACK / SIGN / AJAX / MUFFLER / SHED.
SPILCOM
OIL-SATURATED SOIL INSIDE AJAX SHED. OIL-SATURATED SOIL AROUND BASE OF OIL SKIM TANK. OIL-SATURATED SOIL ON PIT WALLS AND BERMS.
TANKBAT
3-300 BBL UPRIGHTS / BERMED / SIGN / VERTICAL GAS PROCESSORS WITH BIRD PROTECTION / SHED / FLAT SKID-MOUNTED LPG TANK / 300 BBL OIL SKIM TANK / SKIM PIT / PRODUCTION PIT / SHARED BATTERY WITH 005-06818 / DRAINAGE AREA ADJACENT TO PITS.
WELLSIGN
BOTH











Inspection Date: 11/7/2007

Inspection was: Unsatisfactory

Violation: Y

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
ACTION
COVER SKIM PIT. CLEAN UP REMAINING STAINED SOILS AND JUNK.
FIREWALL
BERMS OK
GENHOUSE
JUNK - RODS AND TUBING - ON WELLSITE.
MISC
WELLSITE: PUMP JACK / AJAX WITH MUFFLER AND SHED / SIGN. FOLLOW-UP FOR NOAV # 200119084
SPILCOM
SOIL STAINING NEAR TREATER SHED.
TANKBAT
3-300 BBL UPRIGHTS / BERMED / SIGN / VERTICAL GAS PROCESSORS WITH BIRD PROTECTION / SHED / FLAT SKID-MOUNTED LPG TANK / 300 BBL OIL SKIM TANK
WELLSIGN
BOTH


 
Inspection Date: 11/20/2007

Inspection was: Satisfactory

Field Inspection Comments and Observations

Insp. Comment
Inspection/Violation Comments
FIREWALL
OK
GENHOUSE
OK
MISC
FOLLOW UP TO NOAV INSPECTION--ALL OIL STAINED SOIL HAS BEEN SATISFACTORILY REMOVED FROM BATTERY AND WELLSITE / BERM SEPARATIONS IN PIT HAVE BEEN REMOVED CREATING A SINGLE PRODUCED WATER PIT----PRODUCER MAINTAINS THAT NO SKIM PIT EVER EXISTED---COGCC HAS NO RECORD PERMITTING TWO PITS / ALL OIL CONTAMINATION AS REPRESENTED IN THE NOAV HAS BEEN REMOVED FROM PRODUCED WATER PIT / JUNK AT WELLSITE HAS BEEN REMOVED
SPILCOM
OK






















1 page of over 20 - Analytical Soil Sample Results #3588 to request the entire analytical document, please email us at WTFrack.org@gmail.com







3 comments:

  1. I think this information should be releaced under the Community Right-To-Know Act of 1986.

    ReplyDelete
  2. I never heard of it in the news then.

    ReplyDelete
  3. What happened to the bird????

    Did the Wildlife experts take care of it or did it die?

    ReplyDelete

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